VU Meter replacement on Revox A77

A common issue with old Revox equipment is that the meters get stuck. If you perform an autopsy on these, you'll see that they are built in a very unconventional way, and the problem typically arises when the center magnet (which is glued to the armature) comes loose and does what magnets do: sticks to metal parts. As a result, the moving coil can no longer rotate freely, and the pull can even damage needle bearings, springs, and the windings on the moving coil. Often (with a bit of luck), you can get some glue onto the exposed part of the magnet and carefully rotate the magnet so that its poles are vertical, then pull the magnet back under the armature and center the magnet with a couple of toothpicks as a counterhold. If the poles are swapped, you can just reverse the instrument's terminals; the function remains exactly the same and is associated with less risk than trying to rotate the magnet up to 180 degrees. However, the operation is difficult and always associated with risk, so it's a good idea to continuously check with an ohmmeter to see if the coil is still intact. If the coil wire breaks, the meter is doomed, and there's no point in continuing the project to get the magnet back in place.

In my case, the coil was damaged. But instead of throwing the meter in the trash, I wanted to try to "transplant" a new meter into the original Revox meter.

I bought a cheap 200uA meter on Ali Express. Outwardly, it's ugly and fits poorly (in my case, in a Revox A77).

enter image description here But appearances can be deceiving! Behind the ugly plastic, there is a familiar meter that looks reasonable (better than the original Revox). The meter itself is just pressed into the plastic, so it's not difficult to remove. enter image description here My plan for the transplantation is to keep only the most necessary plastic on the Chinese meter and remove as little plastic as possible from the original Revox meter, aiming for the ideal situation where the two plastic parts can be glued together. Marked in red shows how little plastic remains from the new meter. enter image description here To make room for the "adapter," unfortunately, the Revox meter has to be cut. The new meter is slightly deeper, so there's no room for it unless the bottom is cut free. enter image description here The finished result: The two pieces of plastic can be pressed together and are actually very stable, but a little "sealing" with hot glue does no harm and can seal cracks and protect against dust, metal dust, and thunderflies. There are not room for the bracket, so I cutted them.

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enter image description here The meter on the right is the original. You notice that the pointer on the non-original one is a bit shorter, but it's a cumbersome process to lengthen the needle, and it would also require an extra counterweight if the machine is to stand upright (which my A77 does). I think the result is definitely better than a dead meter. enter image description here

Speaker delay

Vintage DC-coupled Audio Amplifiers do often make a loud "POP!" in the speakes when power is applied. On my Revox A78 I decided to solve this problem by design a speaker-delay circuit that will disconnect the speakers while the DC-output stabilises. I ended up with this schematic: Speaker delay circuit Since the circuit has to be fast reacting when the amplifier is turned on-off, the circuit has to be coupled to the AC-part (secondary winding) of the mains transformer. D4 and C2 will make DC-voltage. The ripple is quite high but sufficient to keep the relay switched without buzzing, but fast reacting when the AC-voltage suddenly disappears (when the amplifier is turned off). No voltage regulation is used, but R1 is used to limit the DC-voltage to +24VDC when the relay is loading the circuit. The relay is placed outside the circuit. Thats makes it easy to use different footprint and near the speaker connections. D1 is a "Flywheel-diode" to avoid damaging some nearby components sensitive to high voltage when the current flow is interrupted. The current flow is controlled by a darlington configuration. The high current gain will make the switching more "consequent" when C1 is charged up by the current, limited by R4. R5 is used to limit the base current though the transistors. The zener diode D3 is used to "extend" the delay time (insted of turning on at C1 = 0,7V+0,7V=1,4V, we have to wait until C1 is charged up to 11,4V. The time constant R4 and C1 is selected long enough so the "POP" can be avoided but short enough to hear when the amplifier is fading in and waking up.
It works well. But one problem is, that C1 won't discharge quickly enough when doing a fast OFF-ON operation. This problem can be solved by making a voltage divider (R2 and R3). When power is applied, the diode D2 won't affect the charging of C1 (since the cathode is higher than the maximum charged voltage on C1). But when the amplifier is turned off, the potential on the cathode of D2 will drop and C1 will be quickly discharged by D2 in series with R3. R2 and R3 is selected to benefit a fast discharge. A fast discharge requires a low R3 and a even lower R2. That much higher requires a high quiescent current. I selected R2=1K and R3=1,2K as a good compromise: 11 mA results in at total power of approx 260 mW (two ordinary 250 mW resistors can be used). Cutting the PCB I cutted and drilled the PCB on my "toy-CNC".

The final results: Yes, some final work has to be done Yes, it needs some final works.

enter image description here I designed the PCB to be attached directly on the bracket, that holds the speaker swich on my A78. Here we also have the AC line for lit up the power-lamp. The relay wire goes back to where the speaker cables goes.

I like the idea. In a non-destructive way, I was able to remove the frustrating POPS in my speakers. I even found a fiberglass PCB with a color similar to the Revox phenolic crap :)

Circuit, PCB-layout, Gerbers (KiCAD) and FlatCAM G-code can be found here

Beogram 3500

I have a Beogram 3500, but unfortunately, it came without the original pickup (MMC 2). I suspect someone removed it for safekeeping and then forgot about it. The MMC is a specialized stylus and cartridge by Bang and Olufsen. However, production ceased when LPs became less common. Nowadays, there are options like "new old stock," replicas, and refurbished needles available. Yet, they can be quite pricey. Given my situation, I require both a new needle and cartridge. I wasn't keen on spending a lot on a functional turntable from the '80s. So, I approached the issue with a mindset: if the repair works out, great; if not, it's not a significant loss.

I disassembled the arm and removed the original, non-standardized cartridge socket.

Disassembly of the arm and breaking/removing the original (non standardized cartridge socket Disassembly of the arm and breaking/removing the original (non standardized cartridge socket).

Messy Beogram 1 Now it becomes quite messy... Messy Beogram 2 I couldn't find a replacement flexible audio cable, so I improvised by twisting magnet wires together. This also served as a makeshift braided shielding. While there might be concerns about impedances and capacities, my main goal was functionality.

enter image description here I then came across an affordable Ortofon 5E pickup. I removed the top of the cartridge mounting fixture (the white part) and soldered the magnet wires directly to the cartridge. Although using proper pin connectors for the cartridge is an option, I decided against it. Gluing the cartridge to the arm makes future replacements challenging anyway. Plus, connectors can lead to unreliable connections. Given that we're dealing with the turntable's critical components, addressing poor connections would be a complex endeavor.

enter image description here After the initial setup, I fine-tuned the cartridge adjustments. It now tracks the record smoothly, and sound is delivered to both channels—achieving my main objective.

enter image description here I then used black cement from our local hardware store to secure the position. An ice cream stick served as a makeshift spatula, smoothing the surface for a cleaner look.

enter image description here objectiveWhile the modifications are noticeable upon close inspection, a casual observer might overlook them. Importantly, the turntable now functions well. Despite the extensive use of putty, soldering, and glue, I've ensured that I can still replace the needle with another from Ortofon's OM series in the future.